This area deserves
a brief write-up. The motor is 220V. I ran 10/3 flexible conduit from
the circuit box, through a double pole switch, and then to the motor.
I was fortunate to have a spool of this stuff from a previous electrical
project. Otherwise, it is probably $50 in wiring. In the circuit box,
which I am fortunate to have right in the shop, I used a double pole
20A breaker. I think I could get away with a 15A double pole breaker,
but I elected to use a 20A. This proved a good idea, because I ended
up having a couple other items operating off these breakers. I added
a low voltage switching system and a fan to cool the motor, both of
which were powered with the dust collection circuit.
I was not satisfied
with having just one switch to turn the collector on, so I replaced
it. I purchased a DPST (Double Pole Single Throw) relay from McMaster-Carr
for $12, which operates with 24 VAC input. Essentially, this is a double
pole switch actuated by the completion of a 24 VAC circuit. So, I wired
right into one of the hot wires of the dust collector circuit a 120VAC
to 24VAC transformer. These are available for about $12 from a hardware
store (your doorbell probably operates with one of these). The reason
you transform this circuit to low voltage is because then you can just
run wires without having to worry about conduit or electrical boxes
and connectors. I then located six total switches in convenient locations
around the shop – two 3-way switches, and four 4-way switches.
I used about 100 ft. of 18/3 thermostat wire to wire all these switches
together so that the dust collector can be turned on or off from anywhere
in the shop.
I chose this system
for two reasons. The first was its cost effectiveness. I was able to
procure the switches and switch plates for free – so this set-up
only cost me $34 for the relay, the transformer, and the thermostat
wire. I didn’t want to spend money on a fancy remote system, and
didn’t think it would fit my needs. Secondly, I didn’t want
to put a switch on every blast gate as some have done. This would mean
that every blast gate has to be closed to shut the system down, and
sometimes I don’t want to have to do that. As well, if I’m
moving from tool to tool, I would have to go open the second tool’s
blast gate, then close the first tool’s blast gate, just so the
motor doesn’t turn off and back on. Not only is this inefficient
because of the extra time it takes, it is also a waste of electricity
(it takes a lot of juice to start a motor over and over again) and is
extremely bad for the motor. I am no expert with electricity or motors,
but I have read that more than 6-10 starts in an hour is horrible for
a motor. It has to do with the capacitors getting too hot, or so I understand.
As well, you can just tell intuitively when you turn this baby on that
the starting phase of the motor is the most painful thing for it.
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One
of six switches located around the shop |
Anyway, my system
of 3 and 4-way switches meets my needs best, reduces the number of times
that the motor gets turned on and off, and I think gives me more flexibility.
The switches are located over the miter saw, over the radial arm saw,
amidst the band saw/belt sander/drill press cluster, in between the
sanding center and the surface planer, above the jointer, and above
the table saw. Basically, they’re located around the perimeter
of the room and one in the middle of the room.
The second item that
was added to the dust collector circuit, and made me glad I used 20A
circuit breakers, was a fan to cool the motor. The motor I used is a
compressor duty motor, and is not designed to be mounted up against
the motor mounting board as it was. They are designed to have air flowing
through them to cool them as they operate. My set-up made it very difficult
for air to flow through this motor. Not only was it mounted up against
a board (it’s actually about 3/16” above the surface of
the motor mounting board because it rests on four small bolt heads that
hold the motor case together, so there’s space for a tiny bit
of air flow), but it was mounted up high in the corner of the shop where
little air flow can get to it. To complicate things, since heat rises,
any heat that the motor creates stays right there in that corner. I
effectively created a self-heating oven for my motor.
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Fan
to cool motor |
Now, this oven takes
a little while to develop - about 25-30 minutes. I noticed it for the
first time when I had the collector on for about an hour, and then it
wouldn’t turn back on because its own internal thermal protection
system wouldn’t allow it. I’m actually surprised it didn’t
just shut itself down, which is what I think these thermal protection
switches are supposed to do, but I’m not sure. In any event, I
wired a fan to turn on when the dust collector does. This fan is aimed
right at the motor and hopefully accomplishes two things. One, it gets
more air flowing through the motor to cool it. Two, it brings cool air
to that upper corner and pushes some of the hot air that may develop
out away from the motor. It does not keep the motor cool, but it does
keep it from getting so hot that it burns up. In the future, I might
put up a fan that can move a larger volume of air to see if it cools
the motor more effectively. As well, in warm weather, I can open the
window behind the dust collector and really create a good ventilation
system through and around the motor.
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